Long day today. Tripp jumped on wiring and I finished some stuff up underneath and routed wires, etc. Tripp's dad came over and made the throttle pedal cable and helped with the rest of the wiring. Richard was here most of the day giving us a hand too. The goal was to have it turn over today.
I was hooking up the starter. Didnt take a picture but it was pretty crusty rusty. Tightening the power wire up, the solenoid plastic just crumbled. So I had to go get a new starter...
We got everything hooked up and put a manual oil pressure gauge on it. With no fuel in the tank we turned it over until we saw pressure. It was firing on the 2.5 year old fuel vapor in the rails, good sign.
Then we rolled it out the door to put fuel in it. The tank wouldn't take gas, so I'll have to rework my venting. I had capped the 5/8" vent, so I pulled that cap and it took fuel.
Then we primed fuel system, checked for leaks, and fired it up.
It's idling at 300 rpm and not taking throttle input. We did a little research and emailed the tuner and it sounds like it's a TAC/ECM mismatch issue. Waiting on a response if it can be fixed in tune.
It's also dripping water from the thermostat housing, so I'll add that to my list.